Evian
Evian
RRCRat Rig Community [Unofficial]
Created by Evian on 4/20/2025 in #fix-my-printer
New Build. VCore 4 failed initial Z-Tilt after homing.
I ended up reflashing my raspberry pi and starting over and that did the trick. I still don't know what the overall issue was but seriously thank you for the assistance!
17 replies
RRCRat Rig Community [Unofficial]
Created by Evian on 4/20/2025 in #fix-my-printer
New Build. VCore 4 failed initial Z-Tilt after homing.
17 replies
RRCRat Rig Community [Unofficial]
Created by Evian on 4/20/2025 in #fix-my-printer
New Build. VCore 4 failed initial Z-Tilt after homing.
Yes. I have verified the endstops.
17 replies
RRCRat Rig Community [Unofficial]
Created by Evian on 4/20/2025 in #fix-my-printer
New Build. VCore 4 failed initial Z-Tilt after homing.
It's off the bed and the Y motor stutters as if it's tryi ng to pull pass the end stop
17 replies
RRCRat Rig Community [Unofficial]
Created by Evian on 4/20/2025 in #fix-my-printer
New Build. VCore 4 failed initial Z-Tilt after homing.
it's asking for a password
17 replies
RRCRat Rig Community [Unofficial]
Created by Evian on 4/20/2025 in #fix-my-printer
New Build. VCore 4 failed initial Z-Tilt after homing.
Ok, Ive cecked and this is what it states: " [z_tilt] z_positions = 0,0 250,500 500,0 points = 30,30 250,460 470,30 horizontal_move_z = 20 retries = 10 retry_tolerance = 0.02 speed = 300 "
17 replies
RRCRat Rig Community [Unofficial]
Created by Evian on 4/20/2025 in #fix-my-printer
New Build. VCore 4 failed initial Z-Tilt after homing.
Everything is up to date and I've checked the printer.cfg which points to the RatOS.cfg. In the [z_tilt] section, it only contains the speed: 300 and that is all.
17 replies
RRCRat Rig Community [Unofficial]
Created by Evian on 4/20/2025 in #fix-my-printer
New Build. VCore 4 failed initial Z-Tilt after homing.
yes, i have
17 replies